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| Topic: Breakdown Information |
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Posted By: mibearbait
on 03/06/06 11:00am
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I had a breakdown this year along I70. I had to call for service using the Newmar Club service. The vendor they sent was able to assist in getting the unit started and I drove it to the nearest truck stop. The truck stop replaced the fuel filter, but this didn't resolve the problem. They checked the computer code, which was a 164-2. They stopped at that point, as the vehicle is still under warranty, they were not authorized to work on Cat engine. We set there for two days waiting for the Cat parts store and service center to open. The local cat dealer determined that the problem was associated with a sensor telling the computer that the engine was having erratic oil pressure, causing the computer to shut the engine down. Sensor was replaced and problem appears to have been resolved.
2004 Newmar Dutchstar Grand Cherokee Toad Garmin 7200 GPS Always remember that you are unique, just like everyone else.
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Posted By: craigpiette
on 03/06/06 03:13pm
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1996 Monaco Exec. purchased used 7/03 attery drain while driving and died as we coasted to a spot of safety ... thought it was alternator ... many hours, new alternator, new batteries, head scratching time later ... the "Isolator" was burnt ... 50 cent piece of wire later it was bypassed and I was headed down the road ::after successful fishing trip deep in Canada rig started to buck then died ... thought it was dirty fuel filters ... after a $1500 tow, diagnosis fuel pump ... 2 days later it arrived ... on down the roadThats all folks! |
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Posted By: Fulltimers
on 03/06/06 10:34pm
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RV particulars: Driveline (Engine, Transmission): Work Horse 8.1, Allison Miles: 12000 Year: 2003 Break Down Description: Hard Start Symptoms: Took 3 tries to start Effect: Once started motorhome ran fine, no power loss, no missing or bucking Cause: Plugged Fuel Filter Outcome: Engine takes 55 psi fuel pressure to start. First try fuel pressure was 30psi, second try fuel pressure was 40psi, third try finally enough psi to start. Once started psi was high enough to run fine. Fulltimers Fulltimers Weblog 2003 Rexhall Aerbus 3550BSL W-22 Workhorse 2005 Saturn Vue (Mr. Toad) 3.5L V6 Automatic
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Posted By: jmbarber
on 03/07/06 08:23pm
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I recently broke down in Mazatlan. The problem was an overheating engine. It turned out that radiator fan stopped working. After several phone calls to Freightliner, I was advised to drain the Dexron III ATF in the hydraulic reservoir, flush the lines and replace the ATF with 15-40 motor oil. It worked! It seems that, in some applications, ATF is a little too thin to turn the fan properly. In my case, the fan stopped but I was able to get it to run again by starting it by hand. It would then run but only at about half-speed...not enough to cool the engine properly. After changing out the ATF for 15-40 engine oil, the fan ran like a wildcat. It seems that some applications need a slightly thicker hydraulic oil to work properly.
Jerry |
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Posted By: mattpoland
on 03/10/06 10:41pm
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RV particulars: 2003 Fleetwood Expedition 38N Driveline (Engine, Transmission): Freightliner, Cummins ISB 300hp, Allison 3000 Miles: 24500 Year: 2003 Break Down Description: Starter failed on my first trip at 24500 miles. This also happened to the original owner on his first trip. My coach has the 3rd starter in it and has less than 30k miles. Symptoms: Effect: Cause: Freightliner says failure both times was from trying to start the motor while the engine was running. Freighliner mechanic says this is common on the ISB's and that the starter is too light duty. Giant RV Murreita delivered a coach with a starter on its last leg twice... Freightliner tried to say it was driver error but so far has paid for it under warranty. Outcome: |
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Posted By: JoeT
on 03/11/06 10:39am
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RV particulars: 2006 Tiffin Phaeton 40 QDH Driveline (Engine, Transmission): CAT C7 350hp, Allison 3000mh Miles: 5426 Year: 2006 Break Down Description: started engine to leave campground. pressed button to retract jacks and heard a loud sound like air escaping. could not get front air pressure to come up with jacks retracted. lowered jacks and front air came up to 120 lbs. retracted jacks and lost air again. Symptoms: low front air pressure with jacks retracted. Effect: air bags would not inflate Cause: quick connect air hose blew off of right front air bag. Outcome: called Coachnet and they sent truck service who reconnected air hose. Joe & Loretta 2012 Winnebago View24M
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Posted By: millikeg
on 03/16/06 10:02am
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RV particulars: 2005 Coachmen Cross Country DP Driveline (Engine, Transmission): Freightliner XC chassis, Cummins 300HP ISB, Allison 2500 (5 speed) Miles: 19,000 Year: 2005 Break Down Description: Last used MH in mid-January. No engine problems since we purchased it new. Early February, MH in driveway, preparing to leave that afternoon for FL. Engine would crank but would not start. No problems of any sort since acquiring new. Called ERS for assistance. They showed up within an hour. Field tech from authorized Freightliner repairer pulled code for "Low Fuel Pressure". He tried for two hours to determine problem. He advised fuel wasn't getting to top of engine and suspected fuel injection pump. Left MH and drove SUV to FL with 6 people in vehicle that night. Upon return from vacation, was towed to repairer's shop. Tech was correct. High Pressure fuel injection pump was replaced. All costs taken care of through warranty. Symptoms: Engine would crank but would not turn over. Check engine light came on. Field tech advised code was for "Low Fuel Pressure". Effect: Had to be towed. Cause: Replaced high pressure fuel injection pump under warranty. Outcome: Everything covered under warranty. Service and level of response from Tri-State Truck in Shrewsbury, MA (authorized warranty shop for Freightliner) was outstanding! * This post was edited 03/16/06 10:10am by millikeg * 2004 Coachmen Sportscoach Elite 402 TS
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Posted By: richardp3
on 03/16/06 04:09pm
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1997 Monaca Dynasty, Cummins 8.3 325hp, 59000 miles. Heading down the road last week to Glen Rose my tach started acting eratic. Pretty soon the tach stopped working altogether. Volt meter reading was just below 12v. I don't know much, but I do know the tach works off the alternator. I knew it wouldn't be too long before the engine used up the batteries. I had the wife crank up the genset and turn on the inverter. This kept us running to our destination and all the way back after the trip was over. Haven't had it fixed yet.
1997 Monaco Dynasty Baron III 38' Me, Her, 3 kids,a dog and a cat.
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Posted By: mattpoland
on 03/28/06 09:21pm
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RV particulars: 03 Fleetwood Expedition 38N Driveline (Engine, Transmission): ISB, 300hp Miles: 31500 Year: 03 Break Down Description: This is a triple slide unit with the Fridge mounted to the inside of the slideout. The fridge is mounted in two places, the front top and the back bottom. The front top mount came undone, pulling the cabinet away from the wall. Effect: Cause: Poor design. Insufficient mounting hardware to handle the weight of the fridge. Outcome: This is a common problem, however, as a second owner Fleetwood will not repair it. The bid to repair to orignial specs is $1000. I am going to take it to another shop or try to find someone to create a better mounting system because I do not want this to happen again. |
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Posted By: lonestarfl
on 03/31/06 03:24am
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Jackjagt wrote: RV particulars: HR Imperial 94 Driveline: Cummins 8.3C, Allison World Miles: 125k Year: 1994 Break Down Description: Sudden power loss, no steering assist Symptoms: Hot dash A/C wiring Effect: hot wires heated the resetable ignition circuit breaker causing engine shut down unexpectedly. This would happen on damp rainy days when I would run the winsheild demist setting on the dash heater/AC. Sudden power loss was traced to curcuit panel under heat vent under dash. Avoided problem by relocated panel to cooler location and moved the "hot curcuit" from below the ignition curcuit. Now refrain from using the winsheild demist setting until I figure out whats causing the dash AC to draw so much current that it heats the wiring so much. Dash AC no longer operative. I would look to see if the AC compressor is on its last leg. My Beaver coach kept tripping the 30a breaker everytime I would turn on the dash AC. Everything look OK on inspection, so we replaced the circuit breaker. Then when the electric clutch on the compressor would engage the wires got warm..pulling in excess of 20a. Once the compressor was replaced the loads went back to normal and the dash air was cold again. Lee |
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