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| Topic: Breakdown Information |
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Posted By: Badeye
on 12/10/03 02:48pm
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Thanks for the inputs. I will start tabulating the data and when we get several, I will put out a summary. Keep them coming. Any breakdowns that you had in the past couple of years will be helpful. Also any new ones, but we hope they are few. If you find several days that I do not chime in, it is because I am on business travel and sometimes do not have internet access if I am traveling international. |
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Posted By: njdirt
on 12/10/03 03:08pm
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add me to the same symptoms and fix as Nantra had except; Ford 460(trans-unsure) 29000 +/- 96 Alegro Bus Bob/Marlene and Crystal(Golden Retriever)and sometimes Grandkids.... 37' Alllego Bay dirts for racing/asphalt's for getting there |
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Posted By: Bartviii
on 12/10/03 03:26pm
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Had just bought used Monaco Windsor, DP and had left Mountain View AR, and had drive approximately 60 miles (in mountains) and got to St. Joe AR on two lane road (Hwy 65) and lost all power. Engine would idle, transmission would shift but throttle pedal had no effect on engine. Called Cummings, and they told me to check the KING CONTROL, which operates remotely from the throttle pedal. I checked it by manually moving the fuel input level and the engine functioned normnally. I called King Controls, who sent me a new one overnight at the cost of @500+. I installed it and it worked fine until I got back to Florida and then malfunctioned again. I again contacted King Control and they sent me another one. I installed that one and it has worked good for two plus years.
Ken & Jo Ann 1997 Monaco Windsor FMCA 188386, 1995 Nissan Pick-up toad |
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Posted By: AlanC
on 12/10/03 04:09pm
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RV particulars:92 Dynasty 36' Driveline (Engine, Transmission): Cummins 8.3 TI 250HP, 6 spd Allison MD3060 Miles:58000 Year:2003 Break Down Description: Catastrophic failure of left front wheel bearing while doing 65 mph, 300 miles after I had paid a F. L. dealer to repack them both sides Symptoms: Felt like a blow out and that I was riding on the rim Effect: came very close to losing control Cause: some ?@$*^!! idiot not doing the job correctly Outcome: Had to have spindle, hub, bearings replaced. Keep both hands on the wheel now at all times, except when stopped. I will now provide service centers with manufacturer's service info (procedures, torques, etc) when having work this done. I will get service facility to write exactly what they did, so I will have documentation. |
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Posted By: waltbens
on 12/10/03 06:14pm
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2001 Winnebago Journey DL. 330 Cat, 3000 MH Allison. Vehicle still very new, near Palmdale, CA. Hit a DIP in the road, after which the front end bottomed. An 8-inch arm had come loose from the anti-dive air valve. Held on by a flimsy grommet; happened 3 more times over 2 years, but I recognized it each time immediately. East to put back on, inboard of the right front wheel. Same trip, the fuel gauge went to "0" in the middle of that desert, 100+ degrees. Kept on truckin'. Started the genset, which ran longer than a minute, telling me the fuel tank/quantity was OK. Next engine start fuel read OK, one air tank read low. It was a CADC or something like that---other indications were low oil pressure. Always something different, till I got to Freightliner. They overnighted one in, no charge. Happened again a year later. Again, overnighted and replaced at no charge. 2003 Imperial, 400 Cummins ISL; '96 Town & Country. Full-timer and loving it. |
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Posted By: Badeye
on 12/10/03 07:17pm
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Please note the original post has been edited. At the suggestion of Big Dave I have added an area for a description of the problem that might aid those who read it. We will continue to improve it until it becomes really useful. Thanks for the help.
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Posted By: strudle
on 12/11/03 08:32pm
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Date of incident July 5, 2003 RV particulars: Sportscoach lll Driveline Chevy 454 turbo 400 Miles:75,000 Year:1986 Break Down Description: Engine Fire Symptoms: Engine Temp Gauge went to zero, about 15 miles from Menomee,MI about 10 miles from town heard "whoossing sound" then when we entered town and stopped at first traffic lite, front of coach was covered up with Smoke & Steam Effect: Engine fire burned wires and vacuum lines on top of engine, carb damaged.Replaced hose section, added water to radiator and drove to a city owned CG. Cause: Heater return hose at engine block ruptured and sprayed a fine mist of engine coolant onto top of engine. Fire started when we stopped at traffic lite. Until that point coolant had vaporized with airflow, but with no airflow when stopped exhaust manifold heat ignited anti-freeze. Outcome: Replaced all hoses & lines on top of engine , replaced carburator, replaced several electrical comnnectors, replaced charcoal canister (fire travelled down hose and blew out bottom of canister) Replaced # 6 & 8 spark plug wires. Insurance job, but we spent 11 days in MI waiting fire inspector and Chevy Dealer to fix it. Strudle 86 Sportscoach lll Bilsteins Safe T Plus Bridgestones |
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Posted By: JDelauter
on 12/12/03 05:53am
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RV particulars: Driveline Cummins 275 Allison 6-spd Miles: 37000 Year:1999 Coachmen Sportscoach Break Down Description: Driving west on I-10, 150 miles from Houston. Engine overheating. Coolant level fine. Slowed to 60 m.p.h. and stopped dash a/c. Made it to California to a Cummins dealer. Split exhaust manifold. Turbo shot. Hole in turbo exhaust pipe. Engine side of radiator blocked with gunk because Freightliiner does not install the road exhaust tube to prevent oil blow-by after moving the radiator to the rear of the engine. Total cost to me: $4300 out-of-pocket. Story gets better as I am headed home (Florida). Bottom line: $7300 from me, zero from extended warranty or Cummins. Symptoms: Overheating Effect: Cause: Outcome Retired SMCM(MDV) USN 30 years 3 'Nam Tours As of 11/04 Full-Timing with: 2003 Gulfstream Friendship, Quad slide 1 lovely wife and 1 sassy Bichon [email protected]
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Posted By: Badeye
on 12/12/03 06:21am
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Spalding12, This is the second thing that I am hoping we can do with this thread if it goes well. If we can start to collect enough data that we can see trends, then my future plans are to contact the manufacturer(s) concerned and share the data with them. Hopefully, they can make sometimes small changes that will prevent further recurrance and maybe we will find some cheap fixes for those of us who have units now. I have already been successful in one instance with one manufacturer. All that was required was the changing of how some wiring was connected, no additional cost to the manufacturer other than changing some drawings and an assembly instruction. This gives me something to do that is productive as I try to wind down my consulting business (not computers or related to the RV business) and have more time available. I have started setting up a database but that is not easy if I want to be able to search out specific problems later. Please keep the information coming. |
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Posted By: wileecoyote985
on 12/12/03 09:47am
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RV particulars: Driveline (Engine, Transmission): Cummins 5.9, Allison 4 spd Miles:58,000 Year:1993 Break Down Description: (You can add any description of the problem here that you think would help others in understanding the situation and problem.) Symptoms: Engine wouldn't start after overnight stay Effect: No start condition Cause: Mis-adjusted shift linkage Outcome: started normally when shifter moved to neutral position. Readjusted linkage after reaching destination. Problem solved. wile e Test pilot for Acme products '93 Southwind DP, Oshkosh Chassis 5.9 190 hp Cummins, 4 spd Allison |
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